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Rear Air Conditioning System Repair

The 1995 S600 comes with a separate rear air conditioning unit built into the center console standard. It was available as an option in other W140 bodies. The unit contains its own fan, evaporator, and a left and right heater core. The left and right side temperatures can be individually adjusted. This feature, combined with the front Climate Control, provides 4 zone climate control in the passenger cabin.

A vent control flap will provide air through the outlet vents, or if it is closed, through the floor vents beneath the front seats. It can be adjusted to provide a mixture between the two as well.

The front AC must be on in order to activate the rear AC. This is because the systems share the refrigerant system. The rear heat function is however stand-alone. In other words, the front heat does not have to be on for the rear to provide heat.

If the left rear occupant wants warmer air than the right rear occupant, they can adjust the air temperature out of the left vent to be warmer. The rear module sees the request for warmer temps, and begins to open left rear duovalve. This valve feeds hot engine coolant to the left rear heater core to warm the air. The duovalve is cycled open and closed to obtain the desired temperature. The longer the valve stays open, the warmer the air becomes. This is called a reheat system, as the air is initially cooled by the shared evaporator if the front AC is on, and then reheated by the rear heater cores.

My car developed a problem with the rear air conditioning unit in the summer of 2005. I first discovered the problem when I noticed that the left rear vent was not blowing as cold as the right rear vent when in AC mode. I performed the onboard diagnostic tests, and got codes indicating a faulty left heater core temperature sensor and open or shorted left rear duovalve. This project outlines what I did to fix the problem.

Tools needed:

  • 5 mm Allen Wrench

  • T10 Torx Bit

  • Small Philips Screwdriver

  • Small Flat Blade Screwdriver

  • 8 mm socket

  • 10 mm socket

  • Socket driver

  • 10 mm closed end wrench

Parts needed:

  • Dependant on your ability and access to services. This project would have normally required replacement of the rear duovalve assembly. I have access to various manufacturing facilities that allow me to repair and overhaul many electrical components. Rebuilding this assembly is possible, but it clearly takes lots of time to do so. If you enjoy analysis and rebuild like I do, give it a shot. If you're not, or are under time constraints, but the new part once you have determined it is bad. 

  • The Duovalve assembly is available for purchase on the internet. I found prices anywhere from $241 to $550.

Time needed:

  • 15 to 20 hours. Keep in mind that this project became fairly involved. The time required to repair this system is also dependant on the exact nature of your problem.

Gently pry the cover from around the vent openings. There are no fasteners, just tabs / prongs that hold it in place.
Insert the 5 mm Allen wrench into the hex bolt behind the vent. 
Unscrew the bolt until it disengages from the air flap. It is a left-hand thread.
Carefully pull the vent out. There are two tabs on the vent that clip into the top of the console. You may need to disengage them using a small flat blade screwdriver. Be careful not to bend them too much, as they can break if old.
Let the vent rest on the drive shaft tunnel.

Inside you will see the air volume control flap, and the left and right heater cores. There is a separating wall between the left and right heater cores. There is a large common evaporator directly beneath the heater cores which is not visible.

Loosen the two small Philips screws holding the rear AC module control to the console.

BE CAREFUL to NOT let the screws drop down into the console. You may never find them. I suggest you stuff a rag into the console to catch them if they fall.

Pull the module out of the console.
Inside you will see the two heater core temp sensors.
Carefully push up on the end of the temp sensor. Give it a little jiggle to help it out of it's socket.

It will come straight up and out.

The complete temp sensor.
Carefully pry the locking tabs of the connector away from the temp sensor, and pull the connector off the sensor.
The sensor is a thermistor assembly. These are resistors that change value depending on ambient temperature.

The temp sensor should provide the following resistances at these temps:

Degrees C               k Ohms 
     10                   19.0 - 21.2
     20                   11.9 - 13.2
     30                   7.7 - 8.4
     45                   4.2 - 4.6

There was nothing wrong with the left temp sensor. To double-check, I pulled the known-to-be-good right temp sensor out and took a resistance reading from it. Both temp sensors were very similar in values.

This was not the best news, as it implied that there could really be a short or open in the left rear duovalve.

Reverse the disassembly steps to put it all back together, but stop just before you're ready to put the vent back in.

Straighten a large paperclip and place it through the hole in the plastic piece as shown.

Reassemble the vent to the console. The paperclip must pass through the bottom of the air vent. The paperclip aligns the female thread so that the 5 mm screw can be installed. Without this, it's just about impossible to get the 5 mm screw started in the female thread.

Make sure all wires are tucked up inside the console and out of the way. If you leave the wires as they are shown in this photo, they will interfere with the vent.

Make sure you do not cross-thread the 5 mm screw into the plastic. The plastic will strip easily if the screw is not lined up correctly.

You will need to adjust the depth of the 5 mm screw to ensure the vent door opens and closes properly.

Now that this is reassembled, it's time to dig out the rear duovalve assembly.

Keep this in mind.

I thought I needed to remove the fender well to get to the rear duovalve assembly. I'm not sure this is necessary. Try removing the panel directly behind the front wheel under the car, and the trim panel behind the front wheel on the side of the car. You may be able to reach the duovalves without having to remove the fender well.

The photos show the fender well removed.

The panels are held on with either 8 mm or 10 mm hex head bolts.

The rear duovalve assembly is tucked behind the middle plastic panel.

I had a heck of a time getting in there even to disconnect the electrical connectors. I couldn't do it. I saw that access would be very simple if I removed the middle trim panel from the fender.

Remove the front 5 fasteners holding the lower body trim to the car.

Open the passenger door, and remove the two bolts securing the middle plastic panel to the front fender.

 

There are three pop-in-place fasteners at the top of the middle trim. Carefully pop the top of the middle trim out of the fender.

There is a hook feature on the trim that grabs the fender near the wheel opening. Gently persuade that free, and the panel should come out.

While holding the lower body trim down out of the way, carefully pull the middle panel out of the slots in the lower trim.
Now the duovalve assembly is easily reached.
The left rear duovalve is circled.
Lots of corrosion apparent. I was hoping that this was the cause of the problem.
There is a nylon tie holding the rubber hoses together. This needs to be cut off.

There are three rubber hoses attached to the valve assembly. One for each valve, and one for the pump (the long part).

Mark the hoses so you know which one went where. Take a flat jaw vice grip pliers or a C clamp, and gently squeeze the hose flat so that no coolant can pour out of it once it's removed from the valve assembly. Clamp where circled in the photo.

Have an old spark plug ready to stuff into the hose to plug it. 

I bought two 3/8" and one 1/2" pipe plugs to cap off the three hoses temporarily.

You will now be able to pull the valve assembly out of the car.

The car is drive-able in this condition.

The area behind the trim panel was full of road dirt. I took the opportunity to clean it out. There is a drain hole, circled, that was plugged up. Make sure you open it up.
After cleaning...
The metal lines for the valve assembly were a bit rusty as well. I cleaned off the rust as much as possible, and painted the lines with a rust inhibiting paint.

I also touched up any rusty areas on the frame and other areas.

Before...

...and after.
The assembly is out and on the work bench. There was quite a bit of corrosion around the unit.
The next step was to verify if there was an open circuit in the left valve. I measured the right solenoid and saw that the coil had continuity as expected.
The left side did indeed show an open circuit. My problem was the left rear duovalve after all.
There are eight T10 fasteners holding the pump and the two bobbin housings to the plastic base of the assembly.

I broke two T10 tips getting 3 fasteners out. The other 5 fasteners were completely seized in the plastic. This surprised me. I didn't think it would be so difficult to get them out.

I removed the pump from the base, and with this removed, I was able to grind the heads of the remaining fasteners off with a Dremel tool (hand grinder).

Carefully pry the bobbin housings from the base using a sharpened spackling knife. Work slowly and carefully. The connector part will come off with the housings.
Pull the two bobbin housings and connector away from the base.
A view of the chambers and passages inside the base. There was some residue and particulates in the passageways.
These two pointy brass parts are the valves. You can see the rubber gasket that is supposed to seal the coils from the coolant.

Again, lots of serious corrosion present.

Remove the valves by pulling them straight up and out.

Remove the rubber gasket as well.

Pull off the intermediate plate. This will expose the coil bobbins.

More corrosion. It is clear that coolant got past the seals and gaskets and into the bobbin area.

Pull the plungers straight up and out.
Another photo of the bobbin area. Major corrosion in this area.
The next step was to get the connector piece off of the bobbin housings. This was tricky. It was not clear how this was attached to the housings.

As you can see by the X-acto knife blade, there is a soft potting compound in the connector cavities.

The connector piece is made of plastic. There is a molded tab that mates with tabs on the bobbin housings. By carefully and gently wiggling and moving the pieces around, I was able to disengage the connector piece from the bobbin housings.

The magnet wire from the coils must be cut from the connector piece to separate the pieces from one another.

Now the coil and bobbin can be pulled out of the bobbin housing.

 

Inspection of the left bobbin coil showed that one of the two wires was broken off. This was the cause of the open circuit. Notice the corrosion on the left wire as well.
Some corrosion and moisture present inside the housing.
Remove the O rings from the intermediate plate, and from the posts inside the bobbin housings.
I then blasted the metal parts with aluminum oxide and glass bead mixture to remove the rust.

I also blasted the metal bracket that the assembly sits on, but remove the three rubber pieces from it first.

The insides of the bobbin housings have a rubber insert in them. I did not try to remove them, as they looked like they were in good shape. They did trap some of the blasting grit though, so I spent a lot of time making sure I got that grit cleaned out completely.

I painted the metal parts with a few coats of clear corrosion resistant enamel, and let them dry thoroughly.

Update 7/230/06...

A fellow MB friend, Dave C., recommends filling any remaining pits with JB Weld (or similar), and filing the surface smooth after it cures. This will recreate a flat surface. It is possible that coolant could leak past gaskets due to poor sealing over pitted areas. Thanks for the comment Dave!

The plastic base was the next problem. Most of the screws holding the components to it had sheared off in the base. I carefully drilled out the broken screws using a 0.040" carbide drill bit, and worked my way up to a #30 bit.

I did not plan on using the same type of fastener. I was planning on using 4-40 stainless steel screws, washers, and nuts to sandwich all the parts together. This turned out to be good, because drilling the old screws out proved to be very challenging.

The bit tips tended to walk off center of the broken screws, which opened the holes in the base. This wasn't going to be a problem because of the different fasteners I was going to use.

Once drilled, I cleaned the base thoroughly to remove all metal chips and residue.

The next step was to determine what size magnet wire was used on the bobbin, and how many turns of wire there was.

I carefully unwound the end wire loop from the bobbin, and began counting as I unwound the wire.

There are 1,150 turns of 28 gage AWS wire, wound CCW looking at the top of the bobbin.

Here is the culprit. The start wire of the winding corroded completely through at the start slot. My guess is that the HML insulation on the wire was scratched through when the coil was wound. Later, as the coil came into contact with coolant, it began to corrode and eventually broke.

Although there are O rings sealing the top and bottom of the bobbins, these components were wet when I disassembled them. It may not be possible to keep them 100% dry in service.

You can see traces of coolant on the bobbin.

The next step is to pick out all the old potting compound from the connector assembly. This is a bit time consuming. Just pick at it slowly with tweezers and a small needle nose pliers. It will eventually all come out.
I wound new coils using 1,150 turns of AWS 28 gage HML magnet wire. This gave a DCR (resistance) of 17.7 ohms.

This worried me because the DCR of the original coils was 15.4 ohms. I was concerned that this difference in resistance would cause faulty operation in the system. I thought perhaps the valves were proportionately modulated during operation. It turns out that these valves operate either fully opened or fully closed. Temperature is controlled by duty cycle, or how long the valve stays open.

The small difference in DCR did not affect operation.

After the coil was wound, I wrapped it with several wraps of adhesive Kapton tape.
The finished coil.
I bought new O rings for the bobbin housings. They are Neoprene 70 compound, which is good for coolant. Size is -016 ( a standard in O rings).
Assemble the coils into the bobbin housings.
Note proper orientation of bobbin inside housing.
Both bobbins in their housings, and the connector attached.
Route the coil wires as shown. Poor quality photo, sorry! See the schematic below for clarification.
This is a schematic of how the coils need to be wired up.

Prepare a small square of sand paper as shown. This will be used to gently strip the insulation off of the magnet wire. The insulation must be removed to solder the wire to the connector terminals.
Carefully sand the insulation off of the coil wires using the sandpaper.

Gently squeeze the sandpaper on the wire, and pull the sandpaper towards the end of the wire. You must hold the left side of the wire (left as pictured) wire to prevent it from being stressed or broken.

Wrap the coil wires around the terminals as shown.
Solder the wires in place.
Place the O rings onto the intermediate plate.
Place the plungers into the bobbins.
Assemble the intermediate plate onto the housings.
I temporarily clamped the plate in place to do some functional testing. I wanted to verify that the valves were working before I continued assembling.

I hooked up 12 volts to the center common terminal.

I then grounded the left and right terminals to verify proper valve action. Note that unenergized, the valves are retracted or open. Applying voltage extends or closes them.

Both valves work as they should. We can continue assembling.

Assemble the rubber gasket, and the valves.
Assemble the bobbin / connector assembly onto the plastic base. I used 1" long 4-40 stainless steel screws, washers, lock washers, and nuts to hold the bobbin housings onto the base.
Next, reassemble the pump to the plastic base. I used three 1.5" long screws for the pump, as they needed to be a bit longer due to the thickness of the pump mounts.

Note proper orientation.

Time to test for functionality again. I repeated my earlier tests, but this time tried to blow through the port under each valve to see if it was opening and closing. Both valves worked fine.
A tip, I keep an old battery charged up just for these kinds of tests. The core value of the battery is $8.00. It's worth more to me to have it on hand to power up 12 VDC devices. I throw it on the charger every now and then to keep it alive.
Now we need to seal up the electrical connections. I used room temp vulcanizing adhesive sealant. I think any kind of water-proof caulking would work though.
Assemble the rubber pieces to the bracket.
Place the duovalve assembly onto the mounting bracket.

Notice that I also cleaned the corrosion off the connector pins.

Make sure the post on the bottom of the plastic base mates with the rubber grommet properly.
Using pliers, gently pull the two rubber mounts up through the holes in the bracket. Make sure they are securing the duovalve assembly to the bracket securely.
Reinstall the assembly into the car. Don't forget to clamp the hoses with a locking pliers to prevent coolant from pouring out.
Start the car, set the rear AC controls for high heat, and let the engine warm up thoroughly. Watch for any leaks on the assembly and on the hoses.

I had to let the car run a good 15 - 20 minutes while playing with the rear AC controls until the air bubbles and pockets were purged from the lines. It took some time for the system to work as expected.

I did hear the valves opening and closing as they should. Once you feel heat and cold the way it should be, you have verified that the system is properly repaired and functioning. Make another visual inspect for any leaks prior to assembling all the body panels.

Good Job! The Rear AC is working again.

 

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